Wednesday, January 18, 2017

The conclusions....



The conclusions of the crash…

Before the NTSB, there was the Civil Aeronautics Board (CAB).  They were the official
agency in charge of investigating the who, what and why of the Holly plane crash.
The post crash investigation at the scene came to no immediate conclusions. The
instrumentation all appeared normal with gauges and readings in their acceptable
parameters.  The engine gave no clues to mechanical failure or loss of power, the
propeller hub upon inspection proved the engine was performing normally at the
point of impact.

There was no part of parts of the wing, or moveable control surfaces
 found far away from the aircraft that might indicate an early departure from the fuselage  before the crash. Upon reviewing the autopsy report of pilot Roger Peterson, nothing remarkable was found that would indicate a medical emergency that would affect his flying senses or motor functions.
His injuries as the other victims were of mass trauma including the head and brain.
The young pilot Peterson was certified to operate under visual flight rules; i.e.
you need to be able to see where you are going. On that particular night, the lack of
a good horizon, low clouds, minimal amount of ground lights in the little populated area
would all make for poor visual flying. Add into the mix some gusting winds, perhaps
a snow squall engulfing the airplane and his not being familiar with the on board gyro
system could bring about spatial disorientation.., thinking you are actually gaining
altitude when in reality you are descending. CAB also mentioned that the weather
briefing was ‘seriously inadequate’ which was given Peterson. To my knowledge the
CAB never attempted to calculate the final weight of the aircraft with its’ passengers,
fuel and luggage.. if the aircraft was overloaded and the center of gravity was
compromised the plane would be severely challenged to fly correctly.  In 2015, the NTSB,
who succeeded the CAB had considered re-opening the crash investigation. That was
proposed by a pilot L.J. Coon, who felt the first conclusions were not correct.
He thought a possible right rudder failure, fuel readings and that improper weight
distribution as mentioned above could be involved. Coon also thought that Peterson
may have tried to land the aircraft, a distinct possibility, and that his efforts should
be noted in the official record. The NTSB in 2016 considered re-opening the
investigation into the crash, but it never happened. And there you have it.

 There are rumors the plane still exists…..and that the Dwyer family has at
least part of it hidden away. (Jerry and Barb Dwyer, were the owners of the airplane.)
Jerry Dwyer passed away in Clear Lake in January 2016. He was writing a book
about the whole affair…his wife has stated she will continue and eventually
finish the book in his memory and honor.

Next and finally; the pistol found at the scene and the years later exhumation

of J.P. Richardson

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